I've been reading about Hydrobowls for years and was hoping I would finish in time to make it to the event about 6 hours from Minneapolis. It is a multi-discipline race with overall winners based on points over 5 races. It is intended to be a measure of overall performance, and I would say it does a reasonably good job at it. The races are a 100m flying start sprint, a slalom, a 100m drag race from standstill, a 2k criterium, and a static thrust test. I wish that there was a race where a fast boat could go fast over a distance without the need for agility, but I suppose this is because I found that my boat was slowest cornering boat of the group!
It is an informal competition, but several of the racers have been going for years, or decades, and have tailored boats to the event and refined over the years. My boat held it's own, but the drive definitely suffered some wear and tear. Before the start I had adjusted the angle of the prop blades to increase the pitch - the distance you are supposed to go each rotation. I ended up with a better feel on the sprint, but the long distance events had me wishing for a faster cadence. I suspect I will go back to somewhere in the middle. The final points totals are pending, but I was somewhere in the middle.
The course is a 100m set of buoys, with two parallel rows. The rows are about 20 meters apart. The slalom weaves between the 5 or so intermediate buoys along the 100m, but you have to span the 20 meters each time. The 2k criterium is 8 1/2 laps around the buoys. This basically means you need a boat that can corner with a 10m turning radius to have any success on these 2 of the 5 events. I would say my boat is more like 20-25m radius. This means the slalom needed some reverse thrust with a paddle to make the turns, and the criterium for me was a lot longer than for everyone else because my oval was about twice as wide as the buoys. My boat turns just fine for cruising a lake, but the 20 degree limit on the rudder rotation means it can't compete on agility.
The drive showed some signs of trouble. I had anticipated both, but there is no good way to know for sure until you just try it. The gearbox skipped teeth in the gears while sprinting. This could be both due to the large size of the housing and the ability of it to flex, but I suspect it is also a result of the bearing bores coming back a little oversize from the shop. The shop ran the reamer at a high RPM and this caused vibrations and a hole that was a little too big. I tried to close it a little by peening edges with a punch to close the opening a little. But it is still not a great fit and allows the output shaft too much play.
Also, I have been using the 25 pitch chain for years without issue on my cat, even after sprints, but this older drive is geared a little higher and also uses 12 tooth sprockets on the prop shaft rather than 9 tooth for the new boat. It doesn't seem like a huge difference, but it means the chain has about 25% more tension during the same pedal force. Given the demands when sprinting, this pushed the boundaries a little too much and the chain started to stretch and get too loose and could get jammed up. Before I could adjust it properly I limped through the slalom and drag race. I wasn't too surprised; I had debated sticking to 12 tooth for a while. I would say the drive would manage just fine for years under normal use, just not all out sprints.
Hard to say where I will head from here in terms of design. The Hydrobowl's future is uncertain since the organizer moved away from the area. It is a fun challenge to tackle an all around boat for these events, but it is hard to say if the events will happen again soon (unless I host one in Minneapolis!). Otherwise I could throw on a new chain and cruise the lake quite content with the way thing are.
This is with the caveat of fixing the stabilizer mounts. As I mentioned, I was concerned about the stiffness after splitting the bracket into two halves. This was a well grounded fear. I've found that the vertical supports behind the seat will rotate slightly and also flex the bracket such that the long supports angle 5-10 degrees (estimating) towards the stern. This means the stabilizer drags at an angle and plows the water, causing more drag and more flexing. During the drag race I crossed a wake and this set off this feedback loop until I almost went for a swim. I will definitely modify this. I am very happy with the vertical adjustment part, but I will join the halves into one. I will also remove the pivoting pieces from the bracket and use a short horizontal double ended nesting tube on the same bracket that connects to both long arms. This will eliminate the flexing. In order to achieve my goal of self contained stabilizers for walking to the lake, I think I will add separate short nesting tubes pointing towards the stern and I can remove the arms from the "in use" tubes and click them onto the "transport" tubes. My timeline for this is uncertain. Fall approaches and it is time to build up a good store of outdoor memories to last through the winter. Fortunately the overall boat is quite sound. I can work on the small stuff like mounting arms and gear boxes in my basement over winter. I'm not sure I will, but at least I could. Come spring, I will get the boat sanded and varnished and actually "finished". Hopefully I will post some more nice cruising photos this month, and then I'll have to wait and see.
Sunday, September 11, 2011
Monday, September 5, 2011
Maiden voyage!
I had my first trials yesterday and today. Generally, they were successful. I had a few bugs to work out with the steering cords and chain tension, but I was on the water doing nice laps after a few false starts. A priority will be grinding the prop to add the lift from a proper profile. Also, I may adjust the pitch as I was spinning out on the pedals before getting to max effort. A future priority will be sealing off a greater portion of the stern hull. You will see the stern sits low due to water that enters a fairly large drive leg stern partition through the drive leg opening. This will be an easy modification once I take the time to work on it. It's been a long day, so I apologize for a lack of a storyline on the trials. This will have to be a photo post for now.
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The rest of the drivetrain
I can say now that the scope of my summer project has been changed slightly. The boat is ready to hit the water (it already has actually, but I'm behind on posts), but it is not finished. I have yet to do any final sanding on the hull; and no varnish yet, either. I will do a few more things to prepare for the Hydrobowl this coming weekend, but I will focus on the prop and steering. Varnish will probably wait until spring. Right now I want to enjoy it for a few weeks before the weather turns. And winters are long here...
The final area of the boat I have not focused on in posts is the rear end of the drive. It is a variation of the flex shaft design Rick has refined lately. I like a lot of advantages of the "standard" flex shaft, but I have had an idea in my head for a few years, and I really wanted to see if it would work. Now that it is mostly done, it is easier to explain. I am using a flexible shaft, for the full length of the boat, but it does not extend below the hull as in Rick's system. I am running the shaft under the seat and along the deck line to the stern where it joins with a separate drive leg. The drive leg uses a 1/4" pitch chain common on twisted chain drives, but the chain does not need to twist since the gearbox has already changed the pedal motion 90 degrees.
After a lot of searching I was able to find inexpensive stainless 9 tooth sprockets for this chain. The max shaft size was 1/4" but I wanted to drill them out for 3/8" shafts. This meant there wasn't enough material left in the hub for a cross pin, so I found a local bicycle fabricator who silver soldered the sprocket on, and it looked pretty secure.
I realize now that my photo collection is incomplete for the drive, but I can add photos later if there are any requests. The shafts are mounted in stainless bearing and I leave it all open to water. This is the same approach I used on my first boat, it is 7 years old now on the original parts with no corrosion on the stainless. Good enough for me. The chain runs through a 1 1/4" OD aluminum tube. This is the smallest possible size drive leg I could figure out how to make. The round tube is welded to a 1 1/4 rectangular tube which houses the prop shaft and bearing.
The drive leg tube has a foil fairing based on precise plywood pieces cut from the CNC batch. I sandwiched foam and wood to maintain and accurate shape. I precut a (slightly undersized) hole in the wood pieces, and once this was all together, I cut it into front and back halves along this hole centerline. I then wrapped sandpaper around scrap tubing and sanded away the foam from the inside. This allowed me to glue the fairing to the drive leg and essentially not add any width to the tube except for a layer of glass cloth.
One of the key reasons this general design appealed to me is that the prop is steerable. The drive leg tube nests inside a square tubing with flange bushings. The drive leg tube has a slot for the upper drive shaft, and the clearance in the slot allows for about 20 degrees of rotation each direction. It can be increased slightly if needed. The square tubing is bolted to the inside of the hull.
One of the primary concerns with drive legs is weed catching and collisions. Generally, these are not issues where I will be boating for the near future, but I added a small strut to help deflect weeds and ramp over obstacles if I hit something. I will eventually file this strut to a nice profile. The twist isn't ideal because it will add slight drag, but it is the fastest approach for now. The bottom of the strut is bolted with a shoulder bolt to the drive leg bottom so the leg can pivot about the strut.
There are plenty of downsides to this design relative to using only a flex shaft under water, and I was aware of them and willing to try it anyway. I accept it is not an ideal solution for most home brew boats. But there are a few advantages, and I will focus on these. Because the shaft only has a small amount of curve, I can use 3/4" diameter (.058" wall) tubing the full distance, and maintain the best possible torsional stiffness with a minimum of weight. I calculate the shaft at about 44 Nm/rad stiffness, significantly higher than cases where a thinner shaft is used underwater to accommodate the increased bending. There is no need for a rudder of any kind, and the strut fairing can be more effective since it is not surface piercing. This is in addition to the steering from prop thrust.
Beaching is more of a gray area. The strut is currently fixed so it will hit when beaching. The lake I am on is deep, so this is not a concern for me. The downside is that the strut is fixed, the upside is that the shaft is protected so beaching will not bend the shaft, which can happen when not using spring steel. In fact, the second reason this design was appealing was that I intended to make the drive leg beach-able. My idea was to detach the stern portion of the hull and add a transom. Then I could use the deck panel or a portion of it to flex up with the shaft. It would essentially be a long hinge flexing/pivoting with the shaft. Since the shaft does not flex a large degree in steady state use, it could accommodate more flex with beaching.
In the end I decided this would take more time, and I would prefer to proof the general concept and reliability before I cut into the boat. If I decide not to continue with this drive leg it is currently easy to undo. If it works out for a year or two, I can still use it as a test bed for a steerable and beach-able flex shaft drive leg.
The complete drivetrain is very low friction. I can easily rotate the shaft with my fingers and maintain motion for about a prop rotation; however, I managed to bend the shaft slightly during my experimenting and it has a slight pulsing as it rotates due to this bend, so it always stops at the high resistance point when I try to spin it. It is not something I can feel with my legs. I replaced my original bushings with ball bearings since they are protected from water. I would consider it relatively light weight as well. The drive leg adds weight but there is no rudder and the shaft has only 12 inches of steel. In the end, the full assembly with full shaft, shaft bearings, drive leg and rudder control is just under 4 lbs.
The final area of the boat I have not focused on in posts is the rear end of the drive. It is a variation of the flex shaft design Rick has refined lately. I like a lot of advantages of the "standard" flex shaft, but I have had an idea in my head for a few years, and I really wanted to see if it would work. Now that it is mostly done, it is easier to explain. I am using a flexible shaft, for the full length of the boat, but it does not extend below the hull as in Rick's system. I am running the shaft under the seat and along the deck line to the stern where it joins with a separate drive leg. The drive leg uses a 1/4" pitch chain common on twisted chain drives, but the chain does not need to twist since the gearbox has already changed the pedal motion 90 degrees.
After a lot of searching I was able to find inexpensive stainless 9 tooth sprockets for this chain. The max shaft size was 1/4" but I wanted to drill them out for 3/8" shafts. This meant there wasn't enough material left in the hub for a cross pin, so I found a local bicycle fabricator who silver soldered the sprocket on, and it looked pretty secure.
I realize now that my photo collection is incomplete for the drive, but I can add photos later if there are any requests. The shafts are mounted in stainless bearing and I leave it all open to water. This is the same approach I used on my first boat, it is 7 years old now on the original parts with no corrosion on the stainless. Good enough for me. The chain runs through a 1 1/4" OD aluminum tube. This is the smallest possible size drive leg I could figure out how to make. The round tube is welded to a 1 1/4 rectangular tube which houses the prop shaft and bearing.
The drive leg tube has a foil fairing based on precise plywood pieces cut from the CNC batch. I sandwiched foam and wood to maintain and accurate shape. I precut a (slightly undersized) hole in the wood pieces, and once this was all together, I cut it into front and back halves along this hole centerline. I then wrapped sandpaper around scrap tubing and sanded away the foam from the inside. This allowed me to glue the fairing to the drive leg and essentially not add any width to the tube except for a layer of glass cloth.
One of the key reasons this general design appealed to me is that the prop is steerable. The drive leg tube nests inside a square tubing with flange bushings. The drive leg tube has a slot for the upper drive shaft, and the clearance in the slot allows for about 20 degrees of rotation each direction. It can be increased slightly if needed. The square tubing is bolted to the inside of the hull.
One of the primary concerns with drive legs is weed catching and collisions. Generally, these are not issues where I will be boating for the near future, but I added a small strut to help deflect weeds and ramp over obstacles if I hit something. I will eventually file this strut to a nice profile. The twist isn't ideal because it will add slight drag, but it is the fastest approach for now. The bottom of the strut is bolted with a shoulder bolt to the drive leg bottom so the leg can pivot about the strut.
There are plenty of downsides to this design relative to using only a flex shaft under water, and I was aware of them and willing to try it anyway. I accept it is not an ideal solution for most home brew boats. But there are a few advantages, and I will focus on these. Because the shaft only has a small amount of curve, I can use 3/4" diameter (.058" wall) tubing the full distance, and maintain the best possible torsional stiffness with a minimum of weight. I calculate the shaft at about 44 Nm/rad stiffness, significantly higher than cases where a thinner shaft is used underwater to accommodate the increased bending. There is no need for a rudder of any kind, and the strut fairing can be more effective since it is not surface piercing. This is in addition to the steering from prop thrust.
Beaching is more of a gray area. The strut is currently fixed so it will hit when beaching. The lake I am on is deep, so this is not a concern for me. The downside is that the strut is fixed, the upside is that the shaft is protected so beaching will not bend the shaft, which can happen when not using spring steel. In fact, the second reason this design was appealing was that I intended to make the drive leg beach-able. My idea was to detach the stern portion of the hull and add a transom. Then I could use the deck panel or a portion of it to flex up with the shaft. It would essentially be a long hinge flexing/pivoting with the shaft. Since the shaft does not flex a large degree in steady state use, it could accommodate more flex with beaching.
In the end I decided this would take more time, and I would prefer to proof the general concept and reliability before I cut into the boat. If I decide not to continue with this drive leg it is currently easy to undo. If it works out for a year or two, I can still use it as a test bed for a steerable and beach-able flex shaft drive leg.
The complete drivetrain is very low friction. I can easily rotate the shaft with my fingers and maintain motion for about a prop rotation; however, I managed to bend the shaft slightly during my experimenting and it has a slight pulsing as it rotates due to this bend, so it always stops at the high resistance point when I try to spin it. It is not something I can feel with my legs. I replaced my original bushings with ball bearings since they are protected from water. I would consider it relatively light weight as well. The drive leg adds weight but there is no rudder and the shaft has only 12 inches of steel. In the end, the full assembly with full shaft, shaft bearings, drive leg and rudder control is just under 4 lbs.
Seat back finished, prop started
As I have mentioned, reworking the seat back has been one of my most time consuming duplicated efforts. My original design had an integrated headrest with a few extra panels to create this. Rick and Mike decided against this in the end for various reasons, including ease of indoor storage, so I too revised this design and cut a new top panel with no head rest. I had this completely built and ready to put on the hull when I decided it was not a good long term solution so I would try the replacement now. I decided to cut the new panels out of cardboard because I barely had enough scrap to use and I could not afford any mistakes. In the end I am happy with the result and would definitely use this shape again. The hatch in this new section is to be fastened with wood screws and is only for maintenance access, not storage.
The gearbox fits in nicely. You might notice that the hole pattern is not perfectly parallel with the slot. I don't think the software is well suited to help a designer verify things like angle between two surfaces. I am quite inexperienced using it, so if there is an easy way, I don't know how, and the end result is my accuracy was off a quarter inch or so. Fortunately the slot was oversized and still had clearance. Once everything was together I could see that the crank arms had about an inch of clearance between the inside of the arm and the boat. It is much more than I needed and it makes my feet farther apart than necessary, but at the time I wasn't sure how far the arms would slide up the tapered shaft, so I erred on the safe side. Now I would cut the shaft much shorter. Incidentally, I also swapped my 170 mm arms for 145 mm arms (I had ordered both at the start to be safe). I have pretty big feet, and it will be very close to hitting my heels on the boat. Someday I will try, but I didn't want delays on my first outing.
I also started my prop using the same folding hub design Rick has been using. In fact, he provided a part I could try. I bent the blades per my design spec, but I did not have time remaining to grind them before we needed to pack up for the holiday weekend. I assembled them to the hub and to the shaft and that will have to do for the first trial.
Time up to this point: My motivation to track accurately is fading, but I am at around 150 hours, including around 20 hours of reworks.
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